Thats my thought. I'm sure for right now i'm going to just get a used std piston, new rings, and the top gasket kit just to have it run....
I looked into the 240 big bore kit and it seems with the weisco piston i can bust out 32HP at least. Which again to me seems like a rather puney number but i've never gone more than the speed of a lawn tractor through a field. I'm sure 17 is still enough to give me some excitement. But i also don't go camping as much as i used to so it won't bother me for this to take time to do. I already enjoy the fact it took less than 20 mins to get the piston out.
I could never do that to a triple..........a stud or cylinder would get stuck
i also found the minimum compression to be 120psi. There's also no rear bumper, there's one someone made thats bent, rear brake switch broken, throttle cable was laying across expansion chamber and melted to steel sheath, no iggy switch, and a few other minor things.
But really with a another piston i don't see whats stopping this thing from running fine. The exhaust port is very slightly damaged but i'm sure it will run "good enough" to at least move about. I'm usually totally against being lazy and i do things the right way but i've got other things going on. Even after what happened i'm still ok with the deal. I'll throw some pics up in a while. Definitely needs some paint, all the plastics have stress bends. Nothing is warped but instead of it being all blue its blue and light blue in spots where the plastic flexed too much.